INTRODUCTION LITERATURE REVIEW METHODOLOGY RESULTS AND DISCUSSIONS

v TABLE OF CONTENT Abstrak i Abstract ii Dedication iii Acknowledgement iv Table of Content v List of Tables x List of Figures xii List of Abbreviations xiii

CHAPTER 1 : INTRODUCTION

1 1.1 Background of Study 1

1.2 Problem Statement

2 1.3 Objectives 3

1.4 Scope of Study

3 1.5 Significance of This Study 4

CHAPTER 2 : LITERATURE REVIEW

5 2.1 Lean Manufacturing LM 5 2.1.1 Lean Principle 6 2.2 Waste 8 vi 2.3 Semi-Structured Interview 9 2.4 Brainstorm 10 2.5 Overall Equipment Effectiveness OEE 10 2.5.1 Calculating OEE 11 2.5.2 Visualizing OEE and the Losses 12 2.5.3 Availability 13 2.5.4 Performance 13 2.5.5 Quality 14 2.6 Six Big Losses 14 2.7 Total Productive Maintenance TPM 16 2.7.1 TPM Implementation 17 2.7.1.1 5S 17 2.7.1.2 Autonomous Maintenance Jishu Hozen 18 2.7.1.3 Planned Maintenance 18 2.7.1.4 Kaizen 19 2.7.1.5 Quality Maintenance 19 2.7.1.6 Training 20 2.7.1.7 Office TPM 20 2.7.1.8 Safety, Health and Environment 20 2.8 Data Collection 20 2.9 Interviews 22 2.10 Observation 22 2.11 Conclusion 23 vii

CHAPTER 3 : METHODOLOGY

24 3.1 Overview of the Methodology 25 3.1.1 The Process Planning Flow Chart 25 3.2 The Explanation of Process Planning Flow Chart 26 3.2.1 Problem Statement Identification 26 3.2.2 Literature Review 27 3.2.3 Identify the Root Cause of Problem 28 3.2.3.1 Semi-Structured Interview 28 3.2.3.2 Brainstorming 29 3.2.3.2Ishikawa Diagram 34 3.2.3.4 Pareto Chart 36 3.2.4 Collecting Data 38 3.2.4.1 Downtime Data Availability 38 3.2.4.2 Daily Production Output Performance 38 3.2.4.3 Accepted Vs Rejected Output Quality 39 3.2.5 Calculating Data 40 3.2.6 Analyzing the Data 40 3.2.6.1 Line Graph 41 3.2.7 Proposing a Solution 42 3.2.7.1 Brainstorm 42 3.3 Conclusion 42 viii

CHAPTER 4 : RESULTS AND DISCUSSIONS

43 4.1 OEE Data Collection 44 4.1.1 OEE Data Collection: Machine C5 and D4 44 4.2 OEE Calculations for Machines 48 4.2.1 Availability 49 4.2.2 Performance 51 4.2.3 Quality 52 4.3 Kaizen Implementation 53 4.3.1 Data Collection Before Kaizen 53 4.3.2 Proposed Solutions 54 4.3.3 Implementation 55 4.3.3.1 Re-Set Pin Rail Gap 55 4.3.3.2 Re-Set the Air Blower Pressure 56 4.3.3.3 Installed Missing Cap Screw 58 4.3.3.4 Upgraded the Vibrator Controller 59 4.3.4 Data Collection After Kaizen 60 4.3.5 Data Analysis 61 4.3.6 Cost 63 4.3.6.1 Cost Loss 63 4.3.6.2 Potential Savings 65 4.4 Conclusions 66 ix

CHAPTER 5 : CONCLUSIONS AND FUTURE RECOMMENDATIONS